roger3645
Petty Officer 1st Class
- Joined
- Aug 30, 2005
- Messages
- 271
Im running a 1975, 850, 85 hp mercury. I previously posted that Im having a problem with the motor cutting off at WOT. Also there was a humming or clicking noise coming from the area of the key switch in the control box. It was suggested that I use a jumper wire to connect the red post to the white on the power pack. So heres what I did.<br /><br /> First I ran sea foam thru using the directions posted. Got quite a bit of smoke the #2 spark plug came out all sparkly and new looking while the other 3 were a bit cleaner but nothing like the number 2 plug. After shutting off the motor I did notice fuel dripping from the bottom carb.<br /><br />I connected a spare control box to the motor and fired it up no more clicking noise from the area of the key switch but the choke button didnt work. But amazingly enough, the tach now works. Hoping this was the problem to end my woes I tried to run her up to 5000 rpms (test tank prop off) Anything past 3K and itll shut down. So then I used the jumper wire red to white, same thing, anything over 3K rpm and shell shut off. Is it the float in the carb flooding out the motor? Or could it be something else. Will do a compression check next weekend.