120 looper from hell....continued

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Hi everyone,

First, let me apologize for the length of this post, but the history and details seem necessary to eliminate some suggestions that have been tried and tested.

I've been busy over the last few weeks working on the beast, but I'm making some headway. It's a 1990 120hp looper J120TLESB that's I bought after sitting for a few years from a fresh top end rebuild. The "mechanic" came highly recommended at the time, now I'd like to smack the guy who said that. I'm finding that the "mechanic" was very sloppy and did a fair amount of butchering on that motor. I'll recap what I've done, but it started with a motor that ran very well above @2000rpm but has a rough idle and seemed to intermittantly drop a cylinder. I couldn't seem to identify the bad cylinder, and thought it might be misfiring on all the cylinders at some point. Sometimes it ran pretty good, but sometimes it would cough and stall. I went through the fuel system, and tested the electrical as best I could without a DVA adaptor. I found the timing seemed to jump a bit and the stator had weak resistance. That was pretty much where we left it last time.


To recap the work (some of this was done prior):

*Compression @ 150, all within a few pounds
*New fuel tank, lines, filter (part of the boat re-build), hoses to and from the pump and primer, no water in system.
*Pulled intake and checked reeds, all looked good and seated with a few showing a glimmer of light through them.
*Found the "mechanic" had used his oldest chisel to scrape off the gaskets and had gouged up the manifolds and backsides of throtle bodies pretty well, some even scratched from edge to edge. I cleaned them up and reinstalled with new gaskets and some sealant for the scratched surfaces. It also seemed that he re-used the old gaskets for the throttle bodies.
*Found possible pinhole leak in plug for VRO, changed it.
*Tested fuel pump and primer, both tested well.
*Carbs spotlessly clean and floats set to perfection
*Butterflies synched to perfection
*Recirc valves and hoses checked
*All other hoses and nipples checked
*Checked all the wires in the harness for wear, all looked good, also replaced most of the regular electrical connectors he had used with heat seal ones. Found some that were pretty corroded up.
*Cleaned up every ground surface ("mechanic" had painted block after the rebuild and didn't bother cleaning the paint off the ground points and behind the starter.)
*Checked thermostats and found port one to be stuck open, changed them both (re-used the diaphragms, they seemed good and weren't cheap-was this a mistake not change them??)
*Regapped plugs (which are Champion QL77JC4,nearly new and clean) to .035" read some threads that said set them to .040 and some said to leave them at .030, so I split the difference.
*Plug wires are new OMC
*Coils are new OMC with clean ground surfaces
*Replaced the stator (new from Outboardparts).
*Replaced the powerpack (unused CDI off ebay for $40. with a guaranty)
*Replaced the timing base (new OMC off ebay $80. still in original box with stocking lable)
*Replaced regulator/rectifier (new CDI from dealer, read threads saying it was a good practice to change with the stator).
*Cleaned up flywheel magnets, all tight, and found a good size sliver of metal stuck in one of the slots on the inner magnetic ring, I suppose this might have thrown off the pickup on the timing base.
*Visually checked the upper bearing cap and seal, the cap was original but the seal was fairly new and looked good. There is some ever-so-slight play in the upper crank bearing, so slight it's hard to tell from rotating movement but it's definitely there. Not sure if a new bearing would be any better, love some input on that. I didn't pull it to check the orings out because I couldn't get a new seal quickly, but he did use some additional sealant on the base when he put it together.
*Lynched and synched
*Set idle timing and WOT timing

There may be more, but that's all I can think of for now. Some of these things I had done before and re-checked. The newer things like the ignition components and intake I didn't do all at once. I started with installing the new stator, powerpack and thermostats at the same time. That resulted in some improvement, especially in the intermittant cylinder drop, which mostly seemed to disappear. It still didn't run smoothly though, and would occasionally still idle up and sputter and die, then run okay again. It also did something new now, when motoring at high speed once, it seemed that the SLOW feature kicked in and held me to 2800 rpms. The temp guage still read cold (when I did the boat over, I unknowingly purchased the temp guage/sender that isn't just for outboards so it barely reads off cold all the time. Cruising throught the site here, I found my mistake too late, but the heads are not overheating, even with the new thermostats I can leave my hand on them after running WOT. It actually seems like the flywheel gets hotter than the heads). After the SLOW kicked in, I felt the heads and they seemed cool enough so I motored on. The motor came right up to speed again and ran fine for some time as I headed in. It did do it again one more time, but oddly kicked me down to 2800 for a few seconds then revved back up. Now I was beginning to think maybe my $40. powerpack was a dud so I put the old one back in to try it. The dropped cylinder problem came back and in testing I was finally able to find that it had a bad wire to #3 cylinder that dropped spark as I moved the orange lead. I put the new powerpack back in and got smoother running again but it seemed to have intermittant weak spark on testing across 7/16", sometimes it would do it, sometimes only @ 1/4". That was when I decided to check all the wiring and grounds and found some issues there (the "mechanic" painted the block after the rebuild, but didn't find the time to clean the paint off the ground surfaces). In that time, I also saw the new OMC timing base on ebay for cheap money so I bid on that and in the down time pulled the intake off and did all that work. I also decided since everything else was new, I should bite the bullet and replace the reg/rect. as recommended. Soooooo, I pulled it down to the block (left the heads on....) and built it back all good and new. Ran it up and it was smooth as glass, like a new motor (I was wearing that sh*t-eatin' grin all night!!!). Took it out the next day with a buddy to set the WOT timing (smooth as glass and running @ 5300 rpm) and it ran perfectly.....for a while. The intermittant running poorly, sputtering, idle came back. I had the timing light and checked the idle again an found it jumping around. I grounded the quickstart lead and it evened out. It also did the SLOW thing again once, for a brief moment, like the feature was switching on and off quickly, and then didn't do it again. The temp gauge still read cool.

Now, with all that done, this is what I'm thinking and I'd love some input. As for the idle issue, it's all electrical. The fuel system is perfect and it runs so smoothly and quietly until it has the problem, which seems to turn on and off like a switch. I also notice when it does act up, the motor is louder with a throaty sound, and the idle is higher. I'm guessing the quickstart is not disengaging and/or kicking in when it's not supposed to. The SLOW issue is new and also intermittant. That would leave it to be a bad powerpack (quite possible, given the purchase) or the temp sensor. I pulled both sensors and tested them with heat. The starboard kicked in @ 165deg and the port kicked the quickstart @ 125deg but the tan lead didn't register until much higher than the 165 of the starboard. It didn't seem to trip at first but eventually did trip though, and my thought would be if anything, it wouldn't be an issue for the idle problem unless it kicked in much lower. I also checked the diode in the tan lead, working fine. I'm leaning towards the new powerpack as the trouble. I purchased finally a DVA adaptor from mastertech (great guys!) and made some tests last night. The adaptor didn't really have much for instructions, but my understanding is that you connect it and set the meter for DC volts. My fluke is digital and auto ranging. I tested using the figures from rapair.com and found the timing base to be well within specs but found some discrepencies with the stator and powerpack:

brwn to brwn/yel: 588 ohms disconnected, 90 volts connected, (should be
950-1100 ohms and 150v- the chart for motors without
quickstart shows 450-550 ohms and 150v)

orng to orng/black: 96 ohms and 17-20v connected or disconnected (chart
shows 93-100ohms and 150v)

orange leads to coils to ground: 175-178volts on all, also, strong blue spark
on all cylinders.

Given these readings, it appears as if the stator is not putting out enough juice, but the spark is very strong and consistant. I assume I'm using the DVA correctly, please let me know if I need to set it differently. I'm going to take her out today and rig it so I can switch off the temp sensor leads for the quickstart and SLOW to see if I can isolate the problem to the sensor or powerpack.

Thanks for any of you who stuck through this long post, and for any input you might have! I think this motor has the potential to be very strong and reliable but it came to me with multiple issues, mostly stemming from some sloppy work. I've eliminated nearly all with lots of help and insight from here, now I can see light at the end of the tunnel.

Evan
 

Dhadley

Supreme Mariner
Joined
Feb 4, 2001
Messages
16,978
Re: 120 looper from hell....continued

A couple of things come to mind. If it truly has 150 lbs compression on each cylinder then it must have small bore heads. Be real careful with that. It's OK but you'll need 93 octane minimum. Or someone has cut the heads and/or deck. Again, be real careful.

Then the flywheel -- you mentioned the magnets are not loose. The V4 outboard uses a non-vented flywheel with cast in magnets. If you're using a vented flywheel with glued in outter magnets and a 35 amp system (from a V4 Sea Drive) you need to verify you have the correct flywheel and ignition system.
 

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Re: 120 looper from hell....continued

Hey Dhadley,

That's pretty interesting on both accounts. The compression was tested with a comp. tester used for diesel motors which has a wide range. The needle was close to the 150 mark and all four were very close to the same mark, but I would say that they could possibly be as low as 140 lbs. I can use another tester to see how accurate the reading was. The guy who did the work only told me that he rebuilt the top end and bored them oversize (he bragged that I should be getting close to 140 hp out of it now, I wrote it off as him trying to sell it...). I'm not sure of the differences of the small bore or cut heads/deck. Would you explain what those would mean, and if there was a way to measure to determine this. Also, would it be a problem to run the 93 fuel if the motor did not have those changes? What are the dangers/problems of having these changes if they are there?

As for the flywhell, he had also mentioned that the motor had a 35 amp system, but the stator and reg/rect numbers cross-referenced into standard 3-9amp. The stator that was in it did look very different from the CDI replacement. The one that came out looked like a solid ring with magnet faces on the sides. The new one looked like individual magnets and sensors connected by the coil. All the wires were the same. The reg/rect. looked the same with the only difference being that the old one had a short red lead that tied into the terminal strip with a red wire coming from the positive battery side of the solenoid. When I installed the new reg/rec. it had a long red lead that CDI tech people said to connect to the same place on the solenoid. That all sound right?

The flywheel is solid with magnets lining the outside of the ring. They are molded into the flywheel and smooth. There is a small smooth magnetic ring around the center hub of the flywheel that has two grooves in it. I wasn't sure when people kept talking about magnets coming loose how mine would, so I assumed mine were "tight". The only way mine could have loosened would be the center ring might have come loose and spun on the hub, but it was tight.
I don't remember seeing a part number on the flywheel, but I can look again. Is there another way of checking whether it is correct if I can't find the number? If it is a 35 amp flywheel, what parts would I have to change to match the system back to 35amp? Are they even available or is it easier/cheaper/necessary to change the flywheel? The motor does time out accurately relative to idle and WOT speeds (although I thought it might run a little higher than 5300).

Lastly, I have some results from my temp sensor isolation today. I made switches to disconnect both tan leads and one that disconnected the white/black while grounding the white/black from the powerpack. The motor did actually seem to run very well with the quickstart grounded all the time. I would occasionally switch it back connected while under way, which I would think would do nothing until the motor was turned off and restarted. It did seem to make somewhat of a difference, but nothing that was remarkable. It actually ran really nice and smooth for the better part of the time I was out. It did run a bit rougher when starting with the quickstart, but it smoothed out like it was supposed to. The tan leads I left connected until the motor kicked down at high speed. It actually didn't do it for almost an hour of hard running, then when I was coming back in at @ 5000 rpm, it started jumping down, then up again. I had my daughter hit the switches to disconnect the tan leads and it made no difference. It was doing it worse than the first time I noticed it, for a longer period of time, surging, so I had her squeeze the fuel bulb and the motor revved right up. We did this several times and without a doubt, squeezing the bulb brought the speed back up. The SLOW feature has been ruled out as a problem, now I'm guessing it's the fuel pump. It looks like the original with the VRO capped. I did loosen the fuel cap to make sure it wasn't a venting issue, and there is no water at all in the tank and filter (took off filter and dumped out, clean fuel only, and then stuck a hose in the fuel tank to suck off the bottom, again clean). The hose and fitting leading from the block to the bottom of the fuel pump were good and tight, but I didn't know how to check the pulse limiter, if that could even be the problem. Does this sound like a classic fuel pump problem? Anything else come to mind that I can check? The motor ran well when I throttled it back down under 4000. But I wonder if it is a fuel pump issue, if it is also affecting the idle. I would expect so, but why intermittantly, and why not mid-throttle?

This is getting to be a real challenge. Every answer seems to lead to new questions! I will win in the end though! Unless, I run out of money first.....

Thanks
Evan
 

Dhadley

Supreme Mariner
Joined
Feb 4, 2001
Messages
16,978
Re: 120 looper from hell....continued

The podded stators are the 10 amp, the ones that you can see the windings are 35 amp stators. The 10 amp flywheel is solid, the 35 amp flywheel has vent holes in it. Sounds like you have a 10 amp flywheel and a 35 stator. That probably won't work. You need to match your ignition system with the correct flywheel.

What are the numbers on the heads? That will tell us if they're big bore (1988 & newer) or small bore heads (85-87). The tab on the head gaskets will tell us what block he used.

Obviously the guy doesn't know what he's talking about. The 120 and 140 powerheads are identical.

All this sounds familiar. Have we talked about this before?
 

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Re: 120 looper from hell....continued

Hi Dhadley,

Yeah, I've been chasing down this rough idle for some time and your advice with the others has been invaluable. In the end, it's probably all for the better. Not only have I learned a whole lot about this motor, I've found numerous little problems along the way and have eliminated them one by one. The more I find, the less impressed I am with the guy who did the work. I'll check out the numbers on the heads tomorrow and get back to you, I'm very curious now. I'll pull my reciepts for the new parts too and run all the numbers to make sure of the ratings. I kept all the old parts so I'll check those numbers too. Also, if I am running the 35 stator with the 10a flywheel, could that account for the lower voltage output of the stator? Amps have an inverse relationship to volts, so higher amps could mean lower voltage, if I remember my high school physics correctly.....

Curious, what are your thoughts on the fuel pump? Squeezing the bulb certainly had an affect. Another separate issue, or possibly related to mismatched ignition?

Thanks,
Evan
 

Dhadley

Supreme Mariner
Joined
Feb 4, 2001
Messages
16,978
Re: 120 looper from hell....continued

If squeezing the bulb improves the performance then the pump probably is getting weak. If it has a leaking diaphram it could lead to flooding or at least putting extra raw fuel in #3 cylinder.

First things first -- you need to determine what parts you really have. What stator? What flywheel? What block? What heads? At some point you'll have to figure out if the carbs are a matched set to the throttle bodies too.
 

steelespike

Supreme Mariner
Joined
Apr 26, 2002
Messages
19,069
Re: 120 looper from hell....continued

As far as the fuel pump issue.You mentiomed the idle raising and then stalling
that is a classic low fuel symtom.Pump replacement sounds reasonable to me.
Looks like the mechanic may have combined parts of a couple of motors.
 

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Re: 120 looper from hell....continued

Hi Guys,

Got some info here. The flywheel part # is 583428, just what the breakdown calls for. The matched stator on the breakdown is 3/9 amp #583410, which was what was in it before I repaced it with a CDI 9amp 173-3410. The flywheel has a ring of holes drilled into it from the top and some smaller ones drilled up from the bottom, but none of the holes connect through. If that's what you meant my porting I'm sorry I didn't understand. I was thinking holes drilled through so air could circulate. The timer base calls for a 583508, which is what I replaced it with, but oddly, the reg/rect. calls for a 584205 but it had a 585192 (looks like for a 130hp 1995-99) in it. I switched it out for a CDI 193-4205 which cross references to both the OMC numbers. The powerpack calls for a 584041, it had a 584040 and I replaced it with a CDI 113-4041 which x-references to both. I can't find any numbers on the carb bodies but the OMC kits I ordered from the breakdown matched the bodies.

From all that, I'm guessing that it has matched ignition parts for a 3/9 amp system. Sound right?

It does get a bit more interesting with the heads though. I can't get any info off the cyl. gasket tabs, they're too small and painted over. They are notched though along the top if that can differentiate them at all. I looked on the block itself and found no numbers. The heads though have distinct numbers cast into them, #333686-1 for starboard & 333686-2 for port. I tried to look them up on the empart site and found no reference. The motor calls for #398818 for both heads. Maybe this will make sense to you. The good news, I imagine, is that I re-tested the compression with a new gauge. All cylinders are pushing 126 lbs +/- 1/2lb. The bad news is I have to tell my brother-in-law that his terribly expensive Snapon tester is off by 25lbs (although it will be fun to see the veins bulge out on his head!). Hopefully, the odd head numbers won't be as significant now. That does leave me with a question about fuel though, what do you guys generally recommend for octane in that motor.

Soooo, if everything seems to be in relative order, I'm looking at changing the fuel pump. Does anyone know the part number for the non-VRO pump conversion? Also, does it mount into the bracket for the old one and do I have to change the pulse limiter as well (included with the pump? part # if not?)? I saw a aftermarket pump on outboardparts.com that sells for @ $215 (part#8402-1 replaces OMC#438402, didn't see a pulse limiter though??) that looks like it might fit the bracket and I could probably get it here a lot quicker than the OMC dealer up the road who knew he didn't have it in stock, but would have to get back to me with a part number and price....still waiting... I like to support the locals, and certainly have over the summer with all the other stuff, but they're not too timely sometimes and the blues are running! Any thoughts on the aftermarket?

Thanks again, I'm curious about the followup to the ignition and cylinder numbers.

Evan
 

Dhadley

Supreme Mariner
Joined
Feb 4, 2001
Messages
16,978
Re: 120 looper from hell....continued

Sounds like the flywheel & stator are correct. The drilled holes are for balancing. The block is a big bore, as it should be. The heads are big bore heads although not a matched set. They're close enough that you'll never see the difference. 125 +/- is more like it. That's why OMC never published numbers. Look for differences not actual numbers.
 

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Re: 120 looper from hell....continued

Thanks Dhadley,

That's a bit reassuring. I wasn't too concerned before you mentioned it about the 150 numbers because they were all the same, but it is good to know that it's within its proper range. Any thoughts on fuel pumps and fuel octane? I found a place that sells the actual 438402 pump for under $200 so I might go that route. It sells as a kit, so do you think/know if the the pulse limiter would be included?

Thanks,
Evan
 

Dhadley

Supreme Mariner
Joined
Feb 4, 2001
Messages
16,978
Re: 120 looper from hell....continued

I've never used that kit (wouldn't be without oil injection) but I'd assume the limiter should be there. If not just get one anyway.
 

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Re: 120 looper from hell....continued

Thanks Dhadley and Steelespike!

I'm going to start a new thread for info on the replacement fuel pump!
 

Mickyfinn

Seaman
Joined
Nov 15, 2005
Messages
65
Re: 120 looper from hell....resolved!!!!

Re: 120 looper from hell....resolved!!!!

Hi guys!

Saturday was a good day. It was the first day my motor has run well since I've owned it! I'd like to say I felt like I've won, but since I've replaced just about every conceivable part on it, it should run good! Thanks to all who've chimed in along the way. It's really been a learning experience for me and you're help has been invaluable. In the end, I've come to the conclusion that there were many small problems from shoddy previous repair work, and a few parts that were gone or on the way out that were the source of all the trouble. Hopefully, I'll get a good run of quality running time before the next issue!

Thanks again,
Evan
 

Dhadley

Supreme Mariner
Joined
Feb 4, 2001
Messages
16,978
Re: 120 looper from hell....resolved!!!!

Re: 120 looper from hell....resolved!!!!

Glad it worked out!
 
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