So i have made other posts about this motor in the past but i want to update that the fatty fifty is now alive once more and runs quite well actually, and as far as fuel consumption goes ot is actually a lot better than i expected especially after i replaced the thermostat (about 12 miles to 6 gal of gas). Anyways i know these motors have a bad reputation for their shift linkage. What do people usually do to correct it? See my current issue is shifting it into forward. It almost acts like the shift rod in the lower unit is too long. I know its not the clutch dog/ cradle or anything in the gearcase itself because i had that all torn apart and inspected. I have all my adjustments advanced as much as they can go but it still doesn't go in all the way, i even took the brass stopper out and ground off about 1/2". When on the boat i can shift into forward but it doesn't feel like it goes in all the way, in fact it slipped out of gear once and went back in. I was considering pulling the lower unit and heating up the shift rod and bending a saddle into it? Would that be advised? Any other suggestions that doesn't involve the scrap yard?
thanks.