Stephen.G.Fiddes
Cadet
- Joined
- Jul 28, 2019
- Messages
- 17
Good Afternoon. I've been round and round with this outboard. When I got it it's fairly low hour, but has had some improperly adjusted parts.
To start, It's running rough. Almost seems like it has a misfire. I'll go through all that I've checked below on muffs
- I have spark on all 3 cylinders. via a spark tester.
- Compression is 124, 125, 128
- Spark plug 1 is fouled and wet, 2 is clean and wet, 3 is lightly fouled and wet
- Carb idle setting is 1 1/16 turn out - (Was 3/4 turn out before, its running marginally better now, tried running it even richer until it got worse, didn't notice a huge change.
- Replaced 1 reed valve block that had 2 damaged reeds - that helped with starting, idle with muffs on hasn't changed.
- Ran unlit propane torch all around the motor, no sign of vacuum leaks. when I put it in front of the carb, it just acted like it was running rich.
- There is some severe popping decelerating from high idle.
I just put it in a bucket of water to watch it idle, and it actually seemed to be idling better. Not perfect, but better. Someone mentioned to me that the backpressure would effect it, and I hadn't even thought of that. (Duh. It's a 2-smoke). Can't really do a high idle or mid-throttle test in the bucket tho.
I know I'm missing some things that I tried. If anyone has any ideas, let me know. I just want this thing running properly so I have a baseline and proper troubleshooting sequence for things.
To start, It's running rough. Almost seems like it has a misfire. I'll go through all that I've checked below on muffs
- I have spark on all 3 cylinders. via a spark tester.
- Compression is 124, 125, 128
- Spark plug 1 is fouled and wet, 2 is clean and wet, 3 is lightly fouled and wet
- Carb idle setting is 1 1/16 turn out - (Was 3/4 turn out before, its running marginally better now, tried running it even richer until it got worse, didn't notice a huge change.
- Replaced 1 reed valve block that had 2 damaged reeds - that helped with starting, idle with muffs on hasn't changed.
- Ran unlit propane torch all around the motor, no sign of vacuum leaks. when I put it in front of the carb, it just acted like it was running rich.
- There is some severe popping decelerating from high idle.
I just put it in a bucket of water to watch it idle, and it actually seemed to be idling better. Not perfect, but better. Someone mentioned to me that the backpressure would effect it, and I hadn't even thought of that. (Duh. It's a 2-smoke). Can't really do a high idle or mid-throttle test in the bucket tho.
I know I'm missing some things that I tried. If anyone has any ideas, let me know. I just want this thing running properly so I have a baseline and proper troubleshooting sequence for things.
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