Fisherg3
Seaman Apprentice
- Joined
- Oct 15, 2021
- Messages
- 41
1990 70hp Johnson 70TLESB
A 2 months ago my motor was running great. Then it began to idle with a terrible but rhythmic shake. But when I had it at WOT it ran smooth but not having a tachometer the only thing I could measure in the difference is speed. My speedometer is digital and gps measured which at its best ran 33kts. It eventually wouldn’t go above 27kts though it sounded the same.
One month ago it began to randomly die at idle after running WOT. It always started right back up. 3 weeks ago I launched started tied it off and ran up my truck. Came down, got in, untied, motor died and I couldn’t get it to start back up again. Ultimately it was a bad cut off switch. But learning as I go. And I seem to be good at doin part replacement jobs throwing new parts and never getting to the issue. Work Summary
Still Need Cutoff Switch and have disconnected the single wire on the power pack that connects to the black and yellow wire.
Finally needed a new starter and it spins the flywheel great now!!
New spark plug wires - not OEM and I believe they are nickle not copper.
New Power Pack
New Control Cables
New Spark Plugs but thought I asked for the Champion QL77JC4 but guy gave me NGK BZ7HS 10 yesterday. Video is from after putting those in. Not sure if this makes a difference.
I two of the fuel line 3 way union connectors had broken due the installing and taking of the carbs. I rebuilt the whole assembly with new T connectors and 5/16 lines. No leaks and primer bulb gets solid
New fuel pump.
New inline fuel filter
I’ve taken off and Cleaned Carbs 3 times and they all have a new gasket, new floats, they are calibrated level but I have issues with getting it to the 3/4 gap when turned upside down. Has a new float, and float valve seat assembly. Each has a new nozzle gasket.
What I do need that fell apart is the Airbox Gasket
*Also - the Orifice Plug that sits behind the drain plug
Of the float bowl on one of them is stuck and found to be mostly gone. What is left is the furthest in portion of the jet so fuel still must travel through the same hole size but again the majority of the Orifice plug is gone. Not sure if this would cause what goes on in the video.
yes I’ve soaked, pinned with wire, sprayed with high volume carb cleaner, and used compressed air to blow out holes.
What the video doesn’t show is it dies. And it’s difficult to start. I have to lift the throttle advance arm at the controls and I have to engage the electric primer
I experienced some bogging in my initial tests last week and pressing in the electric primer Did make it smoothen out. Last night it did make it better but not till after pushing it in for 3 to 4 seconds and only for a minute.
New Gas 50:1 mix (VRO Deleted)
Compression measured Monday at 92 on all three. I read on here that another person was in the 90s and some said it was too low whilst others said for this age and it being 2stroke that it was ok. The other advice i read for the other guy was to test again with a different gauge and this time it read 94 on all 3. Keeping in mind I couldn’t start it so it wasn’t warm. But it’s been super hot here and I measured it when it was over 100° outside temp.
First 2 Videos on the water The motor sounds muffled and echo’y, if you will. I did not hesitate on pushing throttle down or do it slowly. Nor did I pull it back at any given point.
Second two videos detail out what I just now notice about the spark plugs.
Thanks in advance for all the help.
A 2 months ago my motor was running great. Then it began to idle with a terrible but rhythmic shake. But when I had it at WOT it ran smooth but not having a tachometer the only thing I could measure in the difference is speed. My speedometer is digital and gps measured which at its best ran 33kts. It eventually wouldn’t go above 27kts though it sounded the same.
One month ago it began to randomly die at idle after running WOT. It always started right back up. 3 weeks ago I launched started tied it off and ran up my truck. Came down, got in, untied, motor died and I couldn’t get it to start back up again. Ultimately it was a bad cut off switch. But learning as I go. And I seem to be good at doin part replacement jobs throwing new parts and never getting to the issue. Work Summary
Still Need Cutoff Switch and have disconnected the single wire on the power pack that connects to the black and yellow wire.
Finally needed a new starter and it spins the flywheel great now!!
New spark plug wires - not OEM and I believe they are nickle not copper.
New Power Pack
New Control Cables
New Spark Plugs but thought I asked for the Champion QL77JC4 but guy gave me NGK BZ7HS 10 yesterday. Video is from after putting those in. Not sure if this makes a difference.
I two of the fuel line 3 way union connectors had broken due the installing and taking of the carbs. I rebuilt the whole assembly with new T connectors and 5/16 lines. No leaks and primer bulb gets solid
New fuel pump.
New inline fuel filter
I’ve taken off and Cleaned Carbs 3 times and they all have a new gasket, new floats, they are calibrated level but I have issues with getting it to the 3/4 gap when turned upside down. Has a new float, and float valve seat assembly. Each has a new nozzle gasket.
What I do need that fell apart is the Airbox Gasket
*Also - the Orifice Plug that sits behind the drain plug
Of the float bowl on one of them is stuck and found to be mostly gone. What is left is the furthest in portion of the jet so fuel still must travel through the same hole size but again the majority of the Orifice plug is gone. Not sure if this would cause what goes on in the video.
yes I’ve soaked, pinned with wire, sprayed with high volume carb cleaner, and used compressed air to blow out holes.
What the video doesn’t show is it dies. And it’s difficult to start. I have to lift the throttle advance arm at the controls and I have to engage the electric primer
I experienced some bogging in my initial tests last week and pressing in the electric primer Did make it smoothen out. Last night it did make it better but not till after pushing it in for 3 to 4 seconds and only for a minute.
New Gas 50:1 mix (VRO Deleted)
Compression measured Monday at 92 on all three. I read on here that another person was in the 90s and some said it was too low whilst others said for this age and it being 2stroke that it was ok. The other advice i read for the other guy was to test again with a different gauge and this time it read 94 on all 3. Keeping in mind I couldn’t start it so it wasn’t warm. But it’s been super hot here and I measured it when it was over 100° outside temp.
First 2 Videos on the water The motor sounds muffled and echo’y, if you will. I did not hesitate on pushing throttle down or do it slowly. Nor did I pull it back at any given point.
Second two videos detail out what I just now notice about the spark plugs.
Thanks in advance for all the help.
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