CDN BEAVER
Cadet
- Joined
- Jun 29, 2006
- Messages
- 22
Hello Ladies and Gentlemen,
Im currently trying to restore a 1969 Johnson 6hp outboard. Initially the motor would not start or run. I had determined that the cause was due to a stuck needle valve obstructing the flow of fuel to the carburetor. I also found that the fuel pump had obviuosly been taken apart at some point as afew of the springs and dome supports were missing. I replaced the fuel pump, and cleaned and inspected the carburetor until squeeky clean. The motor now starts, idles and seems to run fairly well in the barrel. I decided to mount the motor to the boat and try to take it for a good run.... Like I stated, the motor idles well, but in forward gear, it seems the motor will only run at about 1/4 to 1/3 of its potential speed.
I have removed the spark plugs and they are very black and sooty showing a very rich mixture. I suspect a poor or intermittent spark issue causing the low power. Am I on the right track here? I am in the process of removing the flywheel, but its turning out to be abit stubborn...
Finally I've noticed while running the motor in a barrel, that after the run, there is alot of black oil in the water. Where could this be comming from? I have changed the seals for the fill and drain plugs for the lower unit, and even if the leak were to come from here, I would not expect the oil to be black.
Any help, comments or suggestions are greatly appreciated. Thanks for your time.
Mark.
Im currently trying to restore a 1969 Johnson 6hp outboard. Initially the motor would not start or run. I had determined that the cause was due to a stuck needle valve obstructing the flow of fuel to the carburetor. I also found that the fuel pump had obviuosly been taken apart at some point as afew of the springs and dome supports were missing. I replaced the fuel pump, and cleaned and inspected the carburetor until squeeky clean. The motor now starts, idles and seems to run fairly well in the barrel. I decided to mount the motor to the boat and try to take it for a good run.... Like I stated, the motor idles well, but in forward gear, it seems the motor will only run at about 1/4 to 1/3 of its potential speed.
I have removed the spark plugs and they are very black and sooty showing a very rich mixture. I suspect a poor or intermittent spark issue causing the low power. Am I on the right track here? I am in the process of removing the flywheel, but its turning out to be abit stubborn...
Finally I've noticed while running the motor in a barrel, that after the run, there is alot of black oil in the water. Where could this be comming from? I have changed the seals for the fill and drain plugs for the lower unit, and even if the leak were to come from here, I would not expect the oil to be black.
Any help, comments or suggestions are greatly appreciated. Thanks for your time.
Mark.
