brian3127
Chief Petty Officer
- Joined
- Jun 10, 2007
- Messages
- 507
The primer bulb was replaced by the shop I bought the boat from. Warranty work. Because the old one broke apart and clogged the carbs. So they cleaned the carbs and replaced the primer. That took 2 weeks to fix but anyway that's.long story. Well I get it back today and bring it to the water to go fishing. I squeeze the primer bulb and I hear air at the connection at the motor. I keep squeezing it and now I see gas pouring every time I squeeze it. The bulb never got hard. I get the motor running and me and my son go out. Get past the no wake zone and give it gas. Seems to be running ok. I'm only make about 4000 rpm with a 3 blade prop. Seems low and moving about 17 mph. It's slower than before all of the problems. the motor shut down in the middle of the lake. It started but once I put it into gear it stalls out. So the trolling motor got us home. I guess my question is if I fix the leaky connection will that fix my problem with a new connector or should I bring it back to him because there is more problems other than the connection
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