Yesterday, I fished from 6 a.m. to 5 p.m. I ran the 50 hp Merc off a separate 3 gallon can,
At 6 a.m. I ran 15 minutes at FULL POWER with NO SURGING!
9:30, I ran 5 minutes with NO SURGING,
10:30, as usual, get right up on plane and the SURGING above 4500 rpms returned!!! The problem has been isolated--not connected to the main onboard 31 gallon tank, nor from the 2019 F/W separator.
2 p.m. (air temperature 70 degrees), ran for 10 minutes, still surging above 4500 rpm. These surges are oscillating about 100 rpms,
5 p,m. HOLY COW! I can barely get up on plane! And when I do coax it up, above 3900 rpms the surging is oscillating wildly, swings of about 500 rpms!! Yet if i keep it at 3900 rpm, there's no surging, although just barely enough power to stay up on plane.
A week ago fishing, running off the 31 gallon tank, had similar pattern with one exception:
8 am, usual mild surging above 4500 rpm
4 pm, took a couple minutes to get up on plane. Surging at 4300 rpm.
5 p,m, Not enough steady power to GET UP ON PLANE! After 5 minutes, I gave up trying and went back to fishing with my 6 hp kicker.
7pm, gets right up on plane, mild surging above 4500 rpms.
This problem is deteriorating, gradually worsening. And the "back pressure is building as the use of the 50 hp motor goes. (You can see how, I only use the 50 hp at most an hour per trip,) The 6 hp has a anti siphon valve at the F/W separator output.
Yesterday while the surging was occurring, I placed a brand new CDM for cylinder #3, no effect; then #2, no effect, then #1 cylinder , no effect. BUT what if: 2 of the 3 CDMs are intermittently failing? And then the unburned gas vaporizes in the cylinder creating just enough a "pressure barrier" that has no means to purge, so that by 5 pm, the wild 500 rpm surge swings begin? That doesnt explain how a week ago, at 5 pm (air 80 degrees), I couldnt even get upon plane, So I troll with the 6 hp for 2 hours, then at 7 pm, gets right up on plane with mild surging above 4500 rpms. (air temp maybe 65 degrees)
Last October, with your help I was able to diagnose the trigger failing. I replaced it. Those symptoms gone!
All external gas hoses outside the motor are new. 2 days ago, I replaced the inline fuel filter that is just prior to the 3 carbs. I rebuilt the fuel diaphram 2 days ago. The primer bulb is Quicksilver. I have NOT replaced it---considering the symptoms I don't see how the primer bulb could cause this slwoly worsening (sure seems like an intermittent gradually degrading, worsening problem--
History, I bought this 2005 Smokercraft Osprey, 2005 Mercury 50 hp , 2 stroke, May 2019. The trigger began intermittent failure on June 17th, I replaced the trigger on October 8th.
Mild surging began on 11-22-19 after trolling for 6 hours, 2 pm.. Total hours that I have used this 50 hp = 9 hours.
As of yesterday, 6-17-19 I have runthis 2005 Mercury 2 stroke, 50 hp, a total of 17 hours.