muskyfins
Chief Petty Officer
- Joined
- Jun 7, 2012
- Messages
- 580
Getting ready to head in tonight when the trim wouldn't work. It worked fine on our way out. Trimmed up a bit, got to our anchor spot and sat and relaxed a bit. Getting ready to leave, I always bump the trim up and then down before moving to ensure full down/in. Now trim not working up or down. I've already checked a lot of the usual suspects as detailed below.
2000 Rinker FV270 Mercruiser 5.7 EFI Bravo 3
Trailer switch works. But if the limit switch was out of whack, I'd still have down. (which I don't) Is it safe to eliminate limit switch?
If I jump the low voltage terminal on either solenoid, motor runs fine. So solenoids seem good. This also eliminates the 110 amp fuse.
I disconnected the control disconnect/plug and jumpered each connection individually to eliminate any loss of continuity within the connector. No improvement.
Not only did I replace the control wire fuse, I replaced the fuse holder itself because it was looking gnarly. Fuse wasn't blown anyway. New one doesn't blow either.
Removed the switch from the throttle. Jumped the terminals to bypass switch internals. Pump doesn't run..
I moved enough wiring around that I would have figured any worm insulation/short would have become noticeable.
With boatinfo website down, I do't have a schematic. (been looking at them on other websites) But I'm at a loss. What am I missing? As always any help or thoughts are truly appreciated.
2000 Rinker FV270 Mercruiser 5.7 EFI Bravo 3
Trailer switch works. But if the limit switch was out of whack, I'd still have down. (which I don't) Is it safe to eliminate limit switch?
If I jump the low voltage terminal on either solenoid, motor runs fine. So solenoids seem good. This also eliminates the 110 amp fuse.
I disconnected the control disconnect/plug and jumpered each connection individually to eliminate any loss of continuity within the connector. No improvement.
Not only did I replace the control wire fuse, I replaced the fuse holder itself because it was looking gnarly. Fuse wasn't blown anyway. New one doesn't blow either.
Removed the switch from the throttle. Jumped the terminals to bypass switch internals. Pump doesn't run..
I moved enough wiring around that I would have figured any worm insulation/short would have become noticeable.
With boatinfo website down, I do't have a schematic. (been looking at them on other websites) But I'm at a loss. What am I missing? As always any help or thoughts are truly appreciated.